Today was a day dedicated to the fridge and freezer. I had noticed that the fridge especially had very long run times, and was causing a bit of battery drain. When I had a look at it, the piping outside the actual fridge was covered in ice. This of course seemed a bit wrong, I was obviously wasting quite a bit of energy cooling down the air in the machine room!

So I did a bit of studying. Apparently a cooling system like this needs to have the right amount of carrier gas inside it. If the pressure is not right the system will not work well. Excess icing on the pipes outside the fridge indicates that the pressure is too high. In this case the coolant does not evaporate completely in the evaporator inside the fridge. Thus there is some fluid coolant leaving the fridge, which then evaporates in the pipes on the way to the compressor. This makes the system inefficient.

So all I needed to do to fix the problem was to let a bit of coolant out, which is easy enough. Getting it back in is a different story, so I was very careful in the beginning with how much gas to let out. Working in small increments and waiting maybe 10-15 minutes for the system to stabilize before letting out more.

This image shows the process when it is almost complete. You can see a small length of frost along the pipe in the center. When I started this pipe was completely covered in a thick crust of ice. As more and more gas is let out, the length of pipe that freezes gets shorter and shorter. And in the end the whole visible length of pipe is free from frost.

The compressor now runs significantly shorter times, while keeping the fridge cooler than before. Hooray!


 

Well now I know why the transom compartment bilge pump stopped working ;-) I guess the pump was not as watertight as it was supposed to be. Oh well…


 

This morning was nice and calm. Cloudy, so not as hot as usual. I was working in the transom compartment, trying to find out why the automatic bilge pump had stopped working, when all of a sudden it was not so calm anymore.
An impressive thunderstorm, with gusts of wind up to 45 knots (23 m/s) hit the bay, blowing straight into it. My anchor started dragging pretty badly. The holding in the soft mud here is not so good. And the distance to the leeward shore was only about 300 meter. So I had to get the anchor out in the strong wind, and get the boat turned around before hitting it!

Getting the anchor up when the boat is heaving and turning like this is not so easy, especially when you are alone. I had quite some pulse going before I managed to get it out. By then the boat was drifting sideways to the shore with several knots of speed. This is one of the points in time where you really don’t want the engine to fail ;-)

Well it didn’t, so I got away and managed to put the anchor out again further out in the bay.

By this time the boat was thoroughly soaked inside, since I hadn’t prioritized closing down the hatches. So there was a bit of drying out work to do.

The good side of this incident was that I had a good test of the redesigned anchor arm, which got quite a beating, but held up well. And after calming down somewhat and getting the hatches closed, I also got a good test of the last days work, which was to get rid of the small annoying leaks the hatches had at some of the mounting screws. This test too came out pretty good. The hatches are much less leaky now.


 

It is now too late in the season to continue the journey south. So I am forced to rest a while, waiting until next spring to continue, sometime in September.

One thing that I thought would be fun to do now that I have plenty of time is to write an entry listing some of the problems and issues I have encountered in building this first prototype Journeyman. After all, someone said one of the strengths of mankind is learning from other peoples mistakes. And I know I have a lot of yacht building fans reading this blog. In fact there are over 3 000 people reading it every month.

So. Let’s start with a couple funny design errors: It started with a hole in the bottom that I had designed. The yard workers told me one day one of the aluminum plates for the hull bottom was too short. I couldn’t understand where the error came from until I checked my original design model, and found that there was a 10×80 cm hole in the bottom in front of the keel.  The error had been in the design for over 6 months without me seeing it!

This is the hole:

Another one is the misplaced windows in the forward toilet and showers. The windows are one frame too far aft, which puts half the window in the salon. When I discovered this it was far too late to fix without major rebuilding, so it had to stay that way. Actually very few people notice it, and as a side benefit there is more light in the salon. Anyway, both of these errors were in the original design, despite the several thousand hours I had spent looking at it. Just proves how blind a man can get.

One of the first major problems after launch was the fuel tanks. The manholes in the tank tops were sealed with a sealant that dissolved in diesel. This was of course a very bad idea. Reopening the tanks, removing the sealant and closing them again took about two weeks of completely unnecessary work. But I learned a lot about the chemical properties of various sealants. Sikaflex is not the answer to all problems, after all. There are actually very few sealants on the market that resist modern diesel.

The lifting keel sliders were a similar story. I first used standard marine products, Delrin plastic and Sikaflex glue. Bad choice. Now I have learned a lot about different kinds of plastic and what glues to use. This is a whole science in itself! About two weeks were lost here too, replacing the sliders on the keel. Plus it was pretty expensive.

The last really major design issue was the recent problem with the ballast tanks. But I have already written extensively about that, so I will just mention it here. Of course, that cost almost a month of work and a screwed up sailing schedule.

Not leak testing the hydraulic steering thoroughly enough was a small detail that cost a lot of trouble. It looked good when we put it together in the yard. But now I know that there was almost ten minor leaks in the plumbing. I lost count of how many times I re-bleed the system and filled new oil. Besides a couple of connections that weren’t tight enough, I learned that getting conical thread connections in stainless steel fully tight is difficult. But a little thread-lock glue solved that problem. Another thing that could have spared me many days work if I had done it from the start. But I must say that now that the leaks are fixed, the steering is absolutely fantastic. So precise and smooth, no play at all.

 Smaller things

The mistake with the anchor arm taught me that aluminum is soft. I knew that before, of course. The anchor arm was not supposed to be under load while the boat is at anchor. There is a separate strong eye for that at the bow. But I didn’t think enough about the type of loads the anchor would create when being pulled up. I guess I kind of skipped over that when designing it, it was a detail after all. But one that caused some trouble and also became expensive to fix.

I seem to have chosen too narrow diameters for a few of the drains. For the anchor box and the bathroom wash basins in particular. Narrow pipes flow too slowly and clog easily. An unnecessary problem if I had known it in advance.

I am very annoyed that I made the grab-rail in the ceiling of the deck house too short. This is the only place in the long path from the cockpit to the salon where there is not good enough hold during rough sailing. The rail starts over half a meter away from the entrance door. It would have been very easy to have it start at the door instead. But I didn’t discover this until we were in rough sailing conditions for the first time, and changing it now is a much bigger operation.

At one point in the design process I was pretty bored and didn’t have enough work to keep me fully occupied. So I started to design my own lighting system. This was quite fun for a while, and I still think it will be great, eventually. But with all the other problems that come with building a prototype yacht, I am now regretting this decision. I have not had enough time to make the system work well, and all the salt water that leaked in during the first ballast tank cracking destroyed quite a few of the units in the system. So the system has been kind of limping along for the most part so far, making me wish I had settled for standard products here.

Speaking of standard products, these do cause quite a few problems too. Here are just a few:

I had trouble finding a supplier of deck hatches that was able to make double glassed hatches. I ended up buying from Houdini in England. These hatches are unfortunately shit. The double glassing works well, but the hatches are leaky and the lock and slider mechanisms are always falling apart.

I selected the Vetus dorade ventilators because of their sturdy stainless build, and the good design. I didn’t realize until they were delivered that there was a flimsy piece of plastic holding them together. Dear Vetus, what’s the point of making a ventilator in 3 mm stainless steel if it is mounted in a 2 mm plastic ring that breaks as soon as someone stumbles on it? So I had to dismount and rebuild them with carbon fiber to make them strong. Even worse, when we got out on the ocean for some rough sailing, it turns out that the dorade boxes doesn’t even work. Water flows in despite the boxes. So I have to sail with the ventilators closed all the time to be safe. I have still not figured out a solution to this problem. I might as well no have put any ventilators there at all.

Another disappointment was my Max Power VIP150 bow thruster. Its gearbox broke down completely in the Canary Islands. The supplier did ship me a replacement free of charge, but I have still not mounted it, since this requires getting the boat out of the water. The bow thruster also came with a control unit that was not waterproof, and a control panel where the rubber seals cracked after only a couple of months. Considering the price of this product I think they could have done better.

The list goes on: The wind generator falling down because of badly designed supports. The stove leaking exhausts, and the stove gimbal mount falling apart due to too weak lock washers. The toilet seats falling off because they were mounted with small plastic screws that were too weak. Many hatch locks in the interior loosing their handles because a construction fault cause them to crack inside. It appears to me you pay a premium price for all “marine” products, but they are not always worth it….

Anyways, I think this article is long enough by now. Maybe I’ll continue some other time.


 

Journeyman is now moored in Paraty. I plan to stay here or in the nearby area over the winter. Before writing a couple of longer entries in this blog concerning lessons learned over the last half years sailing, and about future plans, I will just share some cruising experiences from the last weeks.

The area around Ilha Grande, about 70 Nm west of Rio de Janeiro, is considered by many as the very best part of the Brazilian coastline. Ilha Grande has many well protected bays and anchorages in itself, and the small islands and coast around it has a few more. There are no large cities around the bay, so the water is reasonably clear. Well, maybe not just outside the main city Angra dos Reis, but in most other places. So we did a bit of snorkelling and swimming.

There are many beautiful bays like Lagoa Verde above, but in a lot of places the views are spoiled by oil platforms and also a couple of nuclear power plants. Despite this fact, the corals look a lot more healthy than I remember them doing in the Caribbean, for example. Which makes snorkelling quite fun. But you’d better get it done in the morning, because before 11 o’clock loads of tourist charter boats fill up every bay with noise and people. Most Brazilians seem not to know how to swim though, so you can have the deeper waters to yourself…

The small historic city of Paraty is a popular tourist attraction. I have even met a few Swedes. There are loads of small cosy hotels and restaurants. The central parts of the city are closed to cars, so supplies to the stores and hotels are loaded over to carts pulled by horses and mules before they can be delivered.

The national drink of Brazil is of course the Caipirinha, which just happens to be my favourite drink as well. The city of Paraty prides itself as the centre of the Cachaça culture in Brazil, and there is a Cachaça store on almost every block of the city centre. Some sporting several hundred different brands.

At this time of the year it is low season, so the city is pretty dead at nights. This suits me quite well, since I will be working on the boat and less tourists around means I can get things done quicker.


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